OK, I here's the whole story:
I purchased the 2001 from Keith Rutherford in late March of this year (2004). He had just gotten the car back from Elite and had forged internals put in the motor along with some other work. The engine had ~100 miles on it. I have emails from Keith and from Scott stating how strong and reliable the engine would be. However, very quickly the motor started smoking badly. Scott had me do the injector harness upgrade and then every test known to humankind. I have extension email conversations for those who need the gory details. Eventually, I took the car to some good folks up here and with a boroscope discovered a large groove in cylinder #10's liner corresponding with where the wrist pin should be (or not be in a healthy motor). Because of Scott's unresponsiveness (we're 8 weeks into it at this time), we dismantled the motor and found that the wrist pin in #10 had slide out and eaten a fine groove in the liner. Fortunately it didn't get into the block. Anyway Scott had the motor shipped to FL so he could fix it. Finally, it's back - 4 1/2 months later. I've footed the bill for the engine dismantling and at this point, will pay for the reinstallation. Thanks Keith and Scott.
Lou