Scott E. Smith
Enthusiast
just finished putting my 94 R/T back together....but not as easily as it came apart....long story short, it blew a head gasket heads were slightly warped, had them fully machined and block checked for protrusion (ok) used new multilayer gaskets,but when I reassembled, the intake didn't fit anymore!!
had to enlarge bolt holes so it would line up and seal. I think it has too much compression now...somewhat labored starting and runs slightly warmer than before (burped it 4 times to be sure) however seems to have gained some power (quite noticeable!!)the low end I was supposed to loose with the Archer flywheel and headers/exhaust is by no means gone. any input?
had to enlarge bolt holes so it would line up and seal. I think it has too much compression now...somewhat labored starting and runs slightly warmer than before (burped it 4 times to be sure) however seems to have gained some power (quite noticeable!!)the low end I was supposed to loose with the Archer flywheel and headers/exhaust is by no means gone. any input?